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Generation


Tuas Power delivered another year of steady performance in FY07/08. Our steam units maintained a record of 100 per cent reliability. Our Combined Cycle Plants (CCPs) achieved reliability of over 99.9 per cent, with three plants attaining 100 per cent reliability. The ability to sustain this consistent performance is the result of commitment, technical competence and cohesive teamwork within the organisation.


Reliability and flexibility

In our pursuit of operational excellence, we adopted several measures to further enhance reliability and flexibility of our generating units. For instance, we carried out upgrading of the plant maintenance system during the year. We also installed a new GSPL gas tie-line to CCP Blocks 1 and 2 in June 2007 to allow greater flexibility of gas switch. In March 2008, we embarked on a gas compressor project scheduled to be put in service by the end of 2008 to enhance our ability to consume gas from the GSPL gas network.


Best practices

Tuas Power engaged an independent consultant to review the design, engineering and operations of our plant assets in September 2007. The consultant concluded that our level of staffing, training, operations and maintenance programmes are in accordance with good engineering practices in the industry. The review also affirmed that the technology we have in place is sound and proven.

We continue to establish and adhere to high standards in our operations. We were awarded the EMS (Environmental Management System) ISO 14001 certification in April 2007 and the QMS (Quality Management System) ISO 9001 certification in March 2008.


Growing greener

The year saw Tuas Power continue to sustain its environment-friendly operations. In FY07/08 total Carbon Dioxide emissions from our plants were 414g/kWh, which is lower than 418g/kWh registered in the preceding year.

In April 2007, CCP Block 2 underwent a major gas turbine inspection following 48,000 equivalent operating hours. Its combustion system was upgraded to Dry Low Nitrous Oxide (DLN) combustors to reduce Nitrous Oxide emissions, the last unit to complete the upgrading programme.

November 2007 marked the successful commissioning and subsequent takeover of operations and maintenance of our trigeneration facility at Pfizer Asia Pacific Pte Ltd at Tuas Biomedical Park. The first such commercial facility in Singapore, it produces three types of utilities – electricity, steam and chilled water from a single integrated system.

Unlike conventional systems, which convert part of the fuel energy into electricity while the rest is lost as heat, the ‘waste heat’ in a trigeneration system is harnessed to generate steam and produce chilled water. The system is therefore more energy-efficient and environment-friendly. With the escalating cost of energy, this strategic initiative will aid Tuas Power in our efforts to evolve into a leading integrated utility player.